Repair of second HP 3458A metrology DMM


After a year of use in original rusty repaired 3458A it’s advantage in lab and operation performance was obvious and clear. Biggest benefit of this precision DMM is due it’s ultra-high ADC performance and benefits which come from it: Calibration from single 10 V and 10 KΩ standards and ACAL function to remove drift and thermal coefficient errors.

My good friend once mentioned – it’s nice to have at least two pieces of everything. In case of primary reference instrument failure, you still have backup B unit to chase the precision rabbits. While this sounds like a great idea, buying even used good for 3000-5000$ USD DMM just to keep spares is a bold move, especially for hobby home lab. This plan was put on hold, till very recently, when I got a chance to buy another unit. After some seller-related shenanigans, second unit was finally shipped and this repair work-log of second HP 3458A is now possible!

And to follow our best tradition, unit is completely broken and non-functional. Not even photos of power on were possible. There is no fun in buying working equipment. No room for learning how to fix stuff! :)

Manual references

Service notes

There are service notes/engineering changes were published during years of 3458A’s lifecycle. If your unit is old, worth to check if any of them required to do.

Initial photos and conditions

Like a wizard with all-see crystal sphere, here are list (likely not complete) of issues present with the box.

  • Missing A5 PCBA (Outguard controller) Replacement bought and ready
  • Bad VFD? VFD is good and bright
  • Missing top inguard cover. TBC
  • Damaged front panel bezel Replacement ready
  • Scratched display window Replacement ready
  • Damaged front terminal block Will swap with rear. Use triax DIY ports for rear instead.
  • A3 has balanced rundown convergence issue, stops working instantly A3 replacement installed, stable and good!
  • A2 has offsets on all ranges Fixed by recalibration
  • A1 can pass ST/ACAL with good A2/A3 OK

Day 1: Power checks and initial diagnostics

Take a look on that sick box. Understanding is beyound me, how these precision very specialized instruments can end up in shape like this.

Image 1: Front panel

Rear side is okay, nothing bad there, except obvious sign of missing A5 Outguard board with GPIB connector.

Image 2: Front panel

Plastic front panel is literally torn in pieces, just like some angry hulk was hungry. Front panel terminals did not survive the abuse, so that’s a $229 USD right there, if one decide to replace the damaged terminals (Keysight P/N 03458-62111).

Image 3-5: Front panel

Rear terminals are OK, and they are exactly same part as one used in front. So I will move terminal block from rear to front, and use another solution on the rear side. More details to come later in the article about this.

Image 6-8: Front panel

Key rubber pads are not held in place correctly, perhaps due to front panel plastic damage?

Image 9-10: Front panel

FP PCBA is there at least, we can see a VFD glass thru the scratched front panel window.

Image 11: Front panel

Panel plastic is definately going to be replaced. During disassembly it was literally falling apart.

Image 12: Front panel

And now it’s clear why rubber keypads were not in place. Every single FP PCBA locking notch is broken. That is the result of front face impact. Perhaps someone dropped unit on it’s front face? I’m afraid fragile VFD glass is broken.

Image 13-14: Front panel

But VFD glass looks okay. Will see if it’s fully functional upon power up with replacement A5 digital board.

Image 15: Front panel

XFRMR Winding Expected Measured
Red-Red/Yellow 1.8 Ω, 23 VAC 1.73 Ω, 22.8 VAC
Red-Red/Yellow 1.8 Ω, 23 VAC 1.71 Ω, 22.8 VAC
Yellow-Yellow 0.4 Ω, 10 VAC 0.35 Ω, 10.2 VAC
Red-Yellow >10 GΩ OK
Red-Guard >10 GΩ OK
Red-GND >10 GΩ OK
Yellow-Guard >10 GΩ OK
Yellow-GND >10 GΩ OK

Table 1: Transformer test results

Looking good, transformer appear to be healthy. It was quite a pricey part, as we learned during first HP 3458A repair. Schematics of transformer is shown on Image X, in case our readers need a reminder.

Image 16: HP 3458A’s transformer configuration

Now let’s test main power supply rails, both inguard (on A4 PCBA) and outguard (A6 PCBA). If these rails are bad, this could be a disaster and path to the infinite rabbit hole.

Voltage rail Expected Measured
Outguard J400 +5 VDC +5.09 VDC, <3mVpk-pk
Outguard C8 +15 VDC +18.118 VDC, <3mVpk-pk
Outguard U200 +8 VDC +8.12 VDC, <3mVpk-pk
Inguard +5 +5 VDC +5.05 VDC, <3mVpk-pk
Inguard +18 +18 VDC +18.48 VDC, <3mVpk-pk
Inguard -18 -18 VDC -18.68 VDC, <3mVpk-pk

Table 2: Power supply test results

No problems here too, everything is well within spec. Still have a chance for this repair project to be easy and quick? Yeah, I wish. Time will tell.
Time to dig deeper now.

Image 17: Front panel

Day 2 diagnostics, A5 board test and installation

Outguard controller has arrived and ready for initial check and service. This A5 PCBA is newer than Rev.A from original HP 3458A as it’s manufactured in 1996, and features single firmware ROM chip, which is ST M27C4002 in DIP40 package. ROM is UV-eraseable EPROM, so firmware update is possible in field, using UVA-UVC lamp and EEPROM-programmer.

Board P/N is 03458-66505 Rev.B and Engineering Revision tag is 3313. Two-layer PCB made in USA.

Image 18: Front panel

Board came with RAM socket and old 1995-dates Dallas chips, so those are to be removed and replaced with good quality collet sockets, to install fresh new Dallas NVRAMs. RAM on this board formed by pair non-volatile Dallas (today it’s MAXIM) DS1230, high and low bytes separately. If these NVRAM become bad, meter during power-on selftest will throw error RAM TEST 1 LOW or RAM TEST 1 HIGH depends on which IC died and lockup further operation.

Image 19: Front panel

No bodges or issues on bottom side of the board, overall pretty clean.

Image 20-21: Front panel

New DS1230AB and DS1220 installed in sockets, ready for test. I programmed DS1220 with calibration dump from my good 3458A, so I could test operation of this A5 without loosing calibration. Digital boards in 3458A can have different revisions and firmware versions without loosing calibration, as far as calibration ROM is properly transferred between boards.

Image 22-23: Front panel

Firmware is Rev 7. I will update it later to latest Rev.9. Here is collection of firmware ROM dumps for reference:

Firmware ROM dumps for HP/Agilent/Keysight 3458A, read by general purpose ROM programmer. I used TL866CS from eBay to work with firmware ROMs. From information we have, firmware dumps are compatible with all hardware versions.

ROM Revision 2 Revision 4.6 Revision 6 Revision 7 (1992) Revision 8 (1998) Revision 9 (latest)
U110 03458-88820 03458-88840 03458-88860 03458-88870 03458-88880 03458-88890
U111 03458-88821 03458-88841 03458-88861 03458-88871 03458-88881 03458-88891
U112 03458-88822 03458-88842 03458-88862 03458-88872 03458-88882 03458-88892
U113 03458-88823 03458-88843 03458-88863 03458-88873 03458-88883 03458-88893
U114 03458-88824 03458-88844 03458-88864 03458-88874 03458-88884 03458-88894
U115 03458-88825 03458-88845 03458-88865 03458-88875 03458-88885 03458-88895
03458-88877 03458-88887 Single ROM

Table 3: Firmware ROM dumps

Image 24-25: Front panel

Board installed in good 3458A revealed no problems, everything work as expected, including GPIB interface. And to confirm that calibration is not lost or changed, here’s quick GPIB datalog chart, showing LTZ1000 module readout.

Image 26: Front panel

Reading is within ±0.2ppm from original value, prior to A5 board swap.

Since I already installed this fresh A5 in my good meter, I decided to keep it there, so no other hidden issues would arise, while this second sick 3458A will get it’s old A5. There is no functional difference, as both boards running now same Rev.9 firmware.

Day 3 diagnostics, A2 board

As high voltage AC path has incorrect reading, let’s check input HV AC attenuator operation. Schematics fragment from CLIP will be a great help on this.

Image 27: Front panel

First suspects are U201, which is DG211 analog switch, low leakage protection JFETs and zeners Q202,Q203,CR203,CR204 and attenuation network resistors R204,R205,R206,R207,R208,R209.

Day 4, A3 reference measurements

Image 28: Front panel

Measurement of ADC references, which are derived by Linear LT1001 opamps and resistor network inside custom HP ASIC U180, which is famous for main cause of A/D failures and excessive drift.

Image 29: Front panel

Here’s result taken by Keithley 2002 with scanner card and F732B as 10V cross-check reference.

Image 30: Front panel

No need further comments, U180 is dead. These +5, -12, +12 should be fixed ratio of main 7V output of LTZ1000A module A9, but due to bad resistors inside U180 hybrid, we can see large drifts over just few hours of time.

Image 31: Front panel

Also few extra photos were taken

Image 32: Front panel

Image 33: Front panel


Image 34-35: Front panel

Now we need to repeat all that “find-good-A3” quest once again. Anyone still believe it’s possible to get good working 3458A on eBay under 3000-4000$ USD? Cost of A/D PCBA from Keysight service center is around $1300 USD, if reminder is required.

Day 5, A1 Test with good A2 and A3 boards

This board have later upgraded 40.000 KΩ reference resistor, R207 with Vishay VHP101 mark on it, so it’s expected to have less than ±0.3ppm/°C TCR.

Image 36-38: Front panel

Image 39-41: Front panel

Image 42-44: Front panel

Image 45-47: Front panel

To verify correct A1 DC board function faulty original AC Board (A2) and A/D Converter board (A3) were temporarily replaced by ones from good 3458A. This will help us to isolate any issues of A1, and by using verified A2/A3 guesswork is out.

And here we go with first test:

Image 48: Front panel

Surprisingly it passed self-test just fine. Artifact calibration ACAL ALL also went OK, so there is high chance of good condition at least in A1 PCBA. Funny enough, I would rather prefer this board to be faulty than A3, as it’s relatively easy to fix, while with bad U180 hybrid not much we can do.

Next would be test with DCV signal, to make sure it’s all good and stable, before making conclusions on A1.

Day 6-9: New A3 installation and initial tests

After several weeks replacement A3 finally was acquired. There are multiple revisions of A3 board assembly in 3458A units over its 28 years of lifetime.

A3 PCBA Version SKU 03458-66503 Rev.A 03458-66503 Rev.C 03458-66503 Rev.D 03458-66513 Rev.A 03458-66513 Rev.B
Board photograph
First released 1988 1989 ~1995 2000 2015
U180 Hybrid Same package and footprint
Interface MCU 8051 Mask 03458-85501 Rev.2 Mask , ATMEL 8051
U210 Gate array ASIC Fujutsu MB651314 PGA HP 1820-5770 Orbit 6968A PGA Patch PCB 03458-26550 with ALTERA CPLD
Optical interface HP 1005-0097/HP-1005-0096 Avago HFBR-2521Z/Avago HFBR-1521Z
Integrating cap MLCC 50V 50V black plastic NP0 yellow coated MLCC
U213 position 74F112PC HP 1820-2924 IC Jumper pin 8 – pin 10
ADC U142/U405 comparator EL2018CN DIP8 (HP 1826-1817) Patch PCB 03458-66530 with EL2251CM
U404 ramp opamp Hermetic LF400C Plastic LT1122
C401,Q402 Hermetic metal can Plastic
C146,C147 capacitors None Present

Table 4: A3 PCB versions

Image 49-50: Front panel

It’s very recent, according to date codes on ICs made in week 16 year 2016, with most of opamps and logic ICs made in 2015. As Keysight running into more and more difficulties to replace old obsolete parts, they were forced to design patch PCB with P/N 03458-26550 with ALTERA CPLD (RTL code 03458-85550) to replace gate array ASIC with digital logic of A/D converter.

Soldering points around patch boards is still covered in flux and has solder bits, so it’s bit how-ya-doing job there. There is also visible flux around integrating capacitor, perhaps it was selected and replaced after board was originally assembled?

Image 51: ALTERA MAX V 1570Z CPLD A/D control logic

Since used MAX V CPLD is not a direct replacement, without support of 5V logic level, array of Texas Instruments SN74LVC8T245 8-Bit Dual-Supply Bus Transceivers used to interface main A3 PCB signals. There are also two LDOs in center, U11 and U12 with bunch of 0402 and 1210 caps around for decoupling. Three LEDs LD1/LD2/LD3 used for status reporting and unpopulated 6-pin 2.54mm spaced header is likely CPLD JTAG port for ISP.

Backup of gate array CPLD bitstream

Image 52: CPLD label revealed

Test pads on the corner edge are reserved for JTAG connector to handle ISP.

Image 53: CPLD detected with JTAG ISP tool

ALTERA USB Blaster was able to read CPLD configuration without any problems, with dump stored in backup file. Checksum 0056E14F matches one on sticker, so it’s indeed correct dump.

Image 54: Test pad connections using Tek grabbers

Another patch PCB 03458-66530 is installed to replace obsolete Elantec EL2018CN fast ±15V comparator.

Image 55: Elantec comparator patch board

Let’s see if this ADC board is good, as it came untested without any warranty. To do this I’ll run test covered in Service Note SN18 which compares ADC A3 stability versus A9 LTZ1000 reference, assuming later one is good and stable. A week or so of data would be sufficient to tell the initial result.

SN18 ADC stability test

Date/time Meter temperature CAL? 72 CAL? 1,1 CAL? 2,1 Deviation, ppm
18.DEC.2016 20:48 35.5 983.313029E-03 39.9991607E+03 7.07743961 Reference, 0.00
18.DEC.2016 22:35 35.3 983.313077E-03 +0.0488 (0.0488)
19.DEC.2016 08:32 35.5 983.313098E-03 +0.0214 (0.0702)
19.DEC.2016 18:29 35.7 983.313055E-03 -0.0437 (0.0264)
20.DEC.2016 07:48 35.3 983.313080E-03 +0.0254 (0.0519)
20.DEC.2016 18:36 35.7 983.313100E-03 +0.0203 (0.0722)
20.DEC.2016 23:18 35.3 983.313055E-03 -0.0458 (0.0264)
21.DEC.2016 00:56 35.3 983.313155E-03 +0.1070 (0.1281)

Table 5: Initial SN18-stability check

So far initial test revealed no problem, let’s proceed with quick calibration to Fluke 732B 10V DC standard by executing CAL 10.000000 command and repeat same test, together with datalog of 10V. This will let us to see stability with DC signal applied on 10VDC range.

Date/time Meter temperature CAL? 72 CAL? 1,1 CAL? 2,1 Deviation, ppm
21.DEC.2016 09:06 35.5 983.331695E-03 A 39.9991607E+03 7.07037491 Reference, 0.00
21.DEC.2016 20:48 36.2 983.331710E-03 +0.0153 (+0.0153)
22.DEC.2016 08:26 36.2 983.331676E-03 -0.0346 (-0.0193)
23.DEC.2016 00:52 35.6 983.331701E-03 +0.0254 (+0.0061)
23.DEC.2016 08:30 36.0 983.331641E-03 -0.0610 (-0.0549)
24.DEC.2016 17:42 36.2 983.331664E-03 +0.0234 (-0.0315)
24.DEC.2016 18:16 36.1 983.331626E-03 -0.0386 (-0.0702)
24.DEC.2016 23:21 35.5 983.331697E-03 +0.0722 (+0.0020)
25.DEC.2016 16:45 36.6 983.331594E-03 -0.1047 (-0.1027)
26.DEC.2016 01:23 35.2 983.331753E-03 +0.1617 (+0.0590)
26.DEC.2016 08:35 35.4 983.331695E-03 -0.0590 (+0.0000)
27.DEC.2016 03:41 35.2 983.331765E-03 +0.0712 (+0.0712)
28.DEC.2016 11:20 35.9 983.331619E-03 B -0.1485 (-0.0773)
28.DEC.2016 23:32 35.5 983.331704E-03
29.DEC.2016 08:33 35.8 983.331724E-03

Table 6: Post-calibration SN18-stability check

Overall A/D drift rate result per Service Note 18 is [*C = [(A – B) * 1000000] / [A * 7 days] formula*] = -0.0110 ppm, which is well within 0.43 ppm requirement. If this rate is greater than 0.43 ppm/day, then the A3 assembly needs to be replaced.

There is no much repair possible on drifty A3 boards. This is also confirmed by many 3458A owner reports, since usually root cause of excessive drift/integration errors is faulty U180 custom hybrid chip, which is not repairable. Last year I’ve spend more than 200 hours, trying different things to get A3 working in my first 3458A with no avail. Final solution was replacement of A3 PCBA altogether.

Day 10-22: Modification for lower LTZ1000ACH oven temperature

As we will be doing own calibration for this meter, and it’s main use targeted for aircon environment, so very high nominal ~90°C oven temperature of main LTZ1000A-based reference (PCBA A9) is undesired. Higher temperature cause very large long-term drift, which is specified by HP/Agilent/Keysight at 8 ppm/year for standard reference modules and 4 ppm/year for special pre-selected option 002 “high-stability” references. This design decision was made by HP engineers to satisfy +50°C operation temperature range for tight rack-mount usage, such as military applications.

So for metrology and lab purposes this is not good, but solution is rather simple. We can reduce on-die oven temperature of LTZ1000A reference chip by just adding one resistor in parallel with original temperature setpoint one. There is even empty footprint on A9 PCBA, perfectly suitable for this task.

Image 56: Schematics of lower oven temperature tweak

Added resistor need to be high enough value to reduce original X411 15 KΩ resistor down to ~13KΩ which will reduce temperature to ~55°C, improving long term-stability to <2 ppm/°C. Such modification was already successfully performed on my first 3458A and meter indeed is good and stable after the recalibration.

If you change the oven temperature, you will lose the calibration, as the LTZ1000A will change its reference voltage, invalidating previous calibration constants.

Additional resistor has to be high-stability and low tempco type, to ensure that temperature set-point does not drift over time. Vishay Precision Group VAR Z-foil 100 KΩ with specified maximum TCR ±2 ppm/°C resistor satisfy requirements well. Resistor temperature coefficient must be no more than 3ppm/°C. Still most of error comes from original 15 KΩ metal foil resistor, so there is no need for ultra-stable 0.2 ppm/°C resistors unless original one is replaced too. Retail price for VAR BMF resistor range in $USD 15-30 mark, depends on tolerance, value and order quantity required.

Here are few photos of modified LTZ1000 reference, A9 PCBA with 95 KΩ in our first 3458A:

Image 57-58: A9 PCBA modified with Vishay 95KΩ VHP101 resistor for lower oven temperature

And this second unit A9 module, modified same way but with VAR 100KΩ resistor instead:

Image 59-60: A9 PCBA modified with Vishay 100KΩ VAR resistor for lower oven temperature

Now after modification unit was assembled and warmed up few hours to perform stability test once again. No problems revealed at this stage.

Day 23: DC 10VDC test with reference input

Now as we have unit functioning, it’s vital to determine if there is hidden drift over long-term period. And there is no workaround but to actually connect very stable source, such as +10 VDC ovenized DC reference, in this case mighty Fluke 732B and log data over extended period of time, such as week or two. By monitoring deviation and temperature, one can reveal drift component of measured voltage. It’s also important to keep stable environment conditions, such as air temperature/humidity to reduce error from these condition variations.

Image 61: Testing against Fluke 732B standard

To draw a conclusion regarding new A3/meter stability next set of targets should be achieved:

  • Voltage need to be stable within ±0.1 ppm window over 10 minutes of constant TEMP? PASS
  • Stable within ±0.275 ppm window over 24 hour of constant TEMP? PASS, 0.2 ppm
  • Stable within ±0.7 ppm window over 7 days of constant TEMP? PASS, 0.43 ppm
  • Change less than ±0.5 ppm with TEMP? change 5°C PASS
  • Stable within ±1.0 ppm window over 14 days of constant TEMP? PASS

Day 30: Calibration adjustment prior to final test

After stability check next step in repair is calibration adjustment and accuracy testing against know external references. Due to very tight specification for HP 3458A finding “good enough” is often a mighty challenge. However this time opportunity to access stable and well aged Fluke 5700A and calibrated Fluke 732B & ESI SR104 standards was exploited. “Exploit” is correct word here, because meter was located in remote lab for few weeks, with wiring connected between 5700A and our DUT 3458A for days without interferences. Both instruments controlled by Raspberry Pi 3B via GPIB with “linux-gpib and NI GPIB-USB-HS pod”. Environment conditions were logged from “Bosch BME280 THP sensor”.

All equipment was left to warm up and stabilize few days before actual tests ran. Calibration was performed following guidelines in “HP 3458A Calibration manual”. Recently calibrated and well cared DC Standard Fluke 732B was used to execute DC gain calibration, ESI SR104 used for 10 KΩ adjustment, and setup with HP 3325A, Ballatine 1384 3V and 1V thermal converters with nanovoltmeter HP/Agilent/Keysight 34420A.

Day 33: Final calibration tests and report

Day 40-50: Comparisons to other lab gear

Standard under test HP 3458A #1 This HP 3458A #2 K2002 #1 K2002 #2
HI/LO Bias current, 10 DCV, AZERO OFF, ARM HALT pA pA pA pA
+7.1846680 VDC, LTZ1000A, HP A9 STD +7.1846284 [-5.51 ppm] +7.1846288 [-5.45 ppm] +7.1846272 [-5.67 ppm] +7.1846243 [-6.08 ppm]
+7.1298358 VDC, LTZ1000A, KX module +7.1298212 [-2.04 ppm] +7.1298214 [-2.02 ppm] +7.1298195 [-2.29 ppm] +7.1298161 [-2.76 ppm]
+7.1366740 VDC, LTZ1000A, KX module +7.1366613 [-1.78 ppm] +7.1366595 [-2.03 ppm] +7.1366599 [-1.97 ppm] +7.1366570 [-2.38 ppm]
+7.1366450 VDC, LTZ1000A, KX module +7.1366414 [-0.50 ppm] +7.1366398 [-0.73 ppm] +7.1366397 [-0.74 ppm] +7.1366368 [-1.15 ppm]
10V DCV, LTZ1000A, HP 3245A +9.9999596 [-4.04 ppm] +9.9999567 [-4.33 ppm] +9.9999643 [-3.57 ppm] +9.9999512 [-4.88 ppm]
10.00001 KΩ, VPG VHD200 #1 10000.024 Ω [1.4 ppm]
9.999894 KΩ in G9330 body, VPG VHP202 NT 9999.892 Ω [-0.3 ppm]
0.997091 GΩ, DIY STD with Ohmite MOX1125-23

Table 7: Comparisons with our previous 8½-digit DMMs

Also separate set of tests done using Wavetek 4920M as AC voltage standard measurement system.

Standard under test Wavetek 4920M HP 3458A #1 This HP 3458A #2 K2002 #1
10 VAC 1kHz, HP 3245A

Table 8: Comparison with Wavetek 4920M

Day 52: Minor fixes and touch-up

As all functions and operation is confirmed good, I also performed some last minor fixes, such as replacement of all electrolytic capacitors on A6 and A4 power supply boards, replacement of Schaffner mains filter, fan replacement and new front panel installation.

These still intrusive tasks were done after all calibration transfers and main standards measured, to ensure minimal errors on calibration accuracy. Usually any disassembly or repairs, even minor as fan replacement are big no-no after final calibration is done. And exception to this very good rule can be made only if you really know what are the results and ready to loose calibration accuracy. These are not an issue for 1% accurate tool, but remember, no detail is minor once we talking about 1ppm (0.0001%) accuracy!

Thermal infrared images

Thermal analysis and understanding of hot spots and thermal gradients present in metrology-level instrument like HP/Agilent/Keysight 3458A is vital to achieve stable and repeatable ppm-level performance.

HP engineers spend significant amount of resources for overall system design with thermal zoning in play. It is not easy to see this at first glance, but thanks to thermal imagery there are ways to grasp overall key areas of focus. Procedure of capturing images below was next:

  • Meter warmed up for over 24 hours in +25°C ±2°C environment.
  • Outer covers were inplace to ensure thermal distribution as by design.
  • Top cover was removed and thermal photos of A1,A9,A5,A4 boards taken within first 3 minutes by Fluke Ti32 camera.
  • Cover installed back, meter rotated upside and left for 20 minutes to stabilize.
  • Bottom cover removed, photos of A6,A3,A2,A4 taken within 3 minutes.

Image 62: Infrared photo captures

Image 63: More infrared photos


Goal of getting second 3458A in order was achieved, even though actual final effort and cost was way over initial estimated numbers. This is a good lesson to possible volt-nuts, as buying such instrument for low $500 looked like a bargain at first glance, but quickly turned into significant repair expense. It was not unexpected on my part, but there were hopes to avoid expensive A3 board swap.

And this is not considering calibration cost or getting 3458A on Keysight warranty program (which is pricey, but well worth for such expensive instrument). I was lucky to have temporary access to standards and stable calibrator, such as Fluke 5700A to perform own adjustments and calibrations. This also helped to obtain yet another international transfer for DC voltage, resistance and DC current as well as AC calibration for my home lab.

Performing such transfers is key importance to any calibration facility, be it official accredited laboratory or little hobbyist dungeon like mine. Metrology bodies like NIST, NIM, PTB doing same equipment swaps for their “travel” standards and even intrinsic Josephson Voltage standards to build up and maintain confidence in their equipment accuracy and stability. And using 3458A is second-best option (transfer of primary standards would be more accurate, but yet much more risky to ship over half-world) to do simpler transfers thanks to full calibration from just 10 VDC and 10 KΩ reference levels + AC/TVC correction for &mt;1MHz AC.

Project cost:

Item Cost Shipping Supplier
Dead HP 3458A with chewed FP and no A5 PCBA 520$ 190$ eBay
HP 3458A Outguard controller PCBA, Rev.B 400$ N/A eBay
Dallas/MAXIM NVRAMs 1 x DS1220, 2 x DS1230 80$ N/A Maxim
Keysight P/N Cost Qty
03458-40212 Front Panel Sub Assembly $97.50 1
03458-47911 Rear plastic bezel $76.23 1
03458-49331 Window, Front Panel $26.00 1
03458-66513 TBR Analog to Digital In-guard PCA $1306 1

Table 9: Replacement parts orders

Total restoration cost for this meter: $2695.73 USD. Not cheap by any measure, yet still in range of secondary-market value.

Date Activity Time spent
10/28/2016 Received unit, initial teardown and checks 3 hour
10/29/2016 Disassembly and diagnostic checks 2 hour
11/6/2016 Troubleshooting A2/A3 8 hour
11/11/2016 Test A1 with good A2/A3 3 hour
18/12/2016 Testing SN18 start with replaced A3 8 hour
18/12/2016 Testing SN18 start with replaced A3 8 hour
20/12/2016 Modified A9 to lower reference oven temperature with 15KΩ VAR 3 hour
31/12/2016 Meter confirmed good and stable, ready for calibrations 30 hours
04/01/2017 Calibration complete with F732B,SR104 and HP3325A+TVC+F8920A 20 hours
05/01/2017 Calibration report generated using 24h calibrated Fluke 5700A 8 hours
2016-2017 Documentation, photos, article write-up 45 hours

Table 10: Timelog summary

I would like to express my gratitude and appreciation to supporters of this project: Todd Micaleff, Dr.Frank, Kleinstein, plesa and of course all our readers. Stay tuned, many more interesting ideas will be in testing, using fresh duo of Keysight 3458A and Keithley 2002’s real soon.

Author: Illya Tsemenko
Published: Oct. 28, 2016, 2:24 a.m.
Modified: Jan. 27, 2018, 4:01 p.m.
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